Go to the earlier restoration blog.

2/16/19

Moved to the new Lab space.

3/2/19 Hours: 40412.4

We powered up the PDP-9 for the first time in the new lab space. Bit-9 is stuck on in all of the registers so that is the first thing to fix.

3/10/19

We made a longer power cord out of 12-3 SOO cord.

We measured the power consumption at 11A @ 120VAC, so it will $0.30/hour to run the CPU.

We swapped the B131 modules in slots A21 and A23, these are the Adder modules for bits 8 & 9.

The stuck bit moved to bit 8, so we know that the B131 that came out of slot A23 is defective.

We don't have a spare, so we will need to repair it.

3/16/19

The A BUS input on pin S was at -.011V (logic 0) and the other boards were at -3.46 (logic 1).

The SUM output on pin V was at -.3.53V (logic 1) and the other boards were at -0.11 (logic 0).

We measured the input and output voltages on the misbehaving B131 FlipChip, and on the two working neighbors.

Right away we could see that the output voltage was not correct on the broken B131, which explains the stuck bit-9.

The Adder circuitry in the PDP-9 is very fast (for its time), very complicated, and mostly analog.

The internal circuitry has four possible current/voltage levels depending on the state of the four inputs. 

We made a benchtop test setup for the B131 so we could manipulate the input signals and measure the output signals.

Then we compared the behavior of a good B131 to the bad B131.

After a few hours of pondering the schematic to see how it works we were able to devise tests that would show if each of the individual transistors were working correctly.

Eventually we determined that Q4, a 2N3669 transistor was not working at all.

We replaced it with a New Old Stock part, and now the B131 is working again, and the stuck bit-9 is gone.

Alex is making an LT Spice model of this FlipChip so we can better understand how it works.